abac compressor problemsissa brothers parents

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Page 31 Also, please add in your comment the make and model, how old it is, and if you can upload a photo or two, that would help. Neither a leaflet nor a playbook: it is a Catalogue Catalogue. Using it with high speed carving tool, Vortex F5. Every detail at your fingertips! As that would be the only thing that I might see being a possible problem. If so, what make and model of compressor please? im awear my kobalt compressor model 0300841 is out dated what can i do to replace, repair,modifie the regulator. Realign motor pulley with compressor flywheel. Full ABAC Catalogue. 6 Pages. I have the same problem with the same compressor. Receiver does not hold pressure when compressor shuts off. The Pro User's ATF-S Piston range has been designed with ease of use in mind. Further on down the page is a link to a page on this site with links to pages about specific makes or model of compressors. Shamma, only one of the uploads has a video. 64 pages. The first thing Im puzzled about is why an after-cooler? Motor turned on ok from 0 PSI and pumped to 125PSI. "url": "https://www.abacaircompressors.com", I have 1.7 hp,33gal it will fill up one time and will not start for 3hours . Filter by. OK, dont sweat that. So far this is work well for light to med work that I have done. i found some dirty water in the tank and drain it.any help would be appreciated.thank you. Im always pleased to see that someone works out how the compressor works completely, and when modifying, takes that operation into consideration. The other appears to be just a sound file. The evolution of bike maintenance: quick online course, ABAC_2809913206_Angle_grinder_G-202_quickguide_and_DoC, ABAC_2809913403_Chisel_hammer_G-475_quickguide_and_DoC, ABAC_2809913652_Tool_kit_5pcs_G-812IG_manual, ABAC_2809913502_Air_gun_G-503_quickguide_and_DoC, ABAC_2809913253_Orbital_sander_G-250_manual, ABAC_2809913658_Tool_kit_49pcs_G-850_quickguide_and_DoC, ABAC_2809913660_Tool_kit_71pcs_G-852_quickguide_and_DoC, ABAC_2809913659_Tool_kit_66pcs_G-851_manual, ABAC_2809913653_Tool_kit_6pcs_G-813_manual, ABAC_2809913205_Die_grinder_kit_G-201_quickguide_and_DoC, ABAC_2809913300_Combi_nailer_G-301_quickguide_and_DoC, ABAC_2809913500_Air_gun_G-501_quickguide_and_DoC, ABAC_2809913253_Orbital_sander_G-250_quickguide_and_DoC, ABAC_2809913654_Tool_kit_7pcs_G-814B_manual, ABAC_2809913545_Paint_spray_gun_G-551A_manual, ABAC_2809913600_Cartridge_gun_G-570_manual, ABAC_2809913652_Tool_kit_5pcs_G-812IG_quickguide_and_DoC, ABAC_2809913544_Paint_spray_gun_G-550F_quickguide_and_DoC, ABAC_2809913541_Paint_spray_gun_G-541A_manual, ABAC_2809913659_Tool_kit_66pcs_G-851_quickguide_and_DoC, ABAC_2809913653_Tool_kit_6pcs_G-813_quickguide_and_DoC, ABAC_2809913542_Airbrush_kit_G-520_quickguide_and_DoC, ABAC_2809913701_Greasing_gun_G-911_manual, ABAC_2809913402_Chisel_hammer_G-425_manual, ABAC_2809913657_Tool_kit_8pcs_G-810AL-BL_quickguide_and_DoC, ABAC_2809913542_Airbrush_kit_G-520_manual, ABAC_2809913651_Tool_Kit_5pcs_G-811TI_manual, ABAC_2809913600_Cartridge_gun_G-570_quickguide_and_DoC, ABAC_2809913205_Die_grinder_kit_G-201_manual, ABAC_2809913581_Sand_blasting_gun_G-561H_manual, ABAC_2809913650_Tool_kit_8pcs_G-810AL_quickguide_and_DoC, ABAC_2809913581_Sand_blasting_gun_G-561H_quickguide_and_DoC, ABAC_2809913800_Hose_Reel_G-610_10M_Aut._manual, ABAC_2809913105_Impact_wrench_Kit_12_G-101_manual, ABAC_2809913106_Impact_wrench_Kit_12_G-102_quickguide_and_DoC, ABAC_2809913655_Tool_kit_8pcs_G-810P_manual, ABAC_2809913657_Tool_kit_8pcs_G-810AL-BL_manual, ABAC_2809913543_Paint_spray_gun_G-542F_quickguide_and_DoC, ABAC_2809913106_Impact_wrench_Kit_12_G-102_manual, ABAC_2809913206_Angle_grinder_G-202_manual, ABAC_2809913153_Ratchet_wrench_kit_12_G-150_quickguide_and_DoC, ABAC_2809913655_Tool_kit_8pcs_G-810P_quickguide_and_DoC, ABAC_2809913540_Paint_spray_gun_G-540F_manual, ABAC_2809913541_Paint_spray_gun_G-541A_quickguide_and_DoC, ABAC_2809913191_Drill_kit_G-190_quickguide_and_DoC, ABAC_2809913656_Tool_kit_8pcs_G-810P_CEE_quickguide_and_DoC, ABAC_2809913570_Spray_gun_G-530_quickguide_and_DoC, ABAC_2809913301_Stapler_G-302_quickguide_and_DoC, ABAC_2809913572_Watering_gun_G-532_manual, ABAC_2809913544_Paint_spray_gun_G-550F_manual, ABAC_2809913573_Plaster_spray_gun_G-534_quickguide_and_DoC, ABAC_2809913701_Greasing_gun_G-911_quickguide_and_DoC, ABAC_2809913300_Combi_nailer_G-301_manual, ABAC_2809913654_Tool_kit_7pcs_G-814B_quickguide_and_DoC, ABAC_2809913801_Hose_Reel_G-812_9M_Aut._quickguide_and_DoC, ABAC_2809913801_Hose_Reel_G-812_9M_Aut._manual, ABAC_2809913656_Tool_kit_8pcs_G-810P_CEE_manual, ABAC_2809913545_Paint_spray_gun_G-551A_quickguide_and_DoC, ABAC_2809913402_Chisel_hammer_G-425_quickguide_and_DoC, ABAC_2809913571_Spray_gun_G-531_quickguide_and_DoC, ABAC_2809913153_Ratchet_wrench_kit_12_G-150_manual, ABAC_2809913105_Impact_wrench_Kit_12_G-101_quickguide_and_DoC, ABAC_2809913660_Tool_kit_71pcs_G-852_manual, ABAC_2809913252_Palm_sander_G-225_quickguide_and_DoC, ABAC_2809913580_Sand_blasting_gun_G-560A_quickguide_and_DoC, ABAC_2809913572_Watering_gun_G-532_quickguide_and_DoC, ABAC_2809913622_Tire_inflator_G-580_quickguide_and_DoC, ABAC_2809913573_Plaster_spray_gun_G-534_manual, ABAC_2809913651_Tool_Kit_5pcs_G-811TI_quickguide_and_DoC, ABAC_2809913658_Tool_kit_49pcs_G-850_manual, ABAC_2809913580_Sand_blasting_gun_G-560A_manual, ABAC_2809913800_Hose_Reel_G-610_10M_Aut._quickguide_and_DoC, ABAC_2809913622_Tire_inflator_G-580_manual, ABAC_2809913650_Tool_kit_8pcs_G-810AL_manual, ABAC_2809913543_Paint_spray_gun_G-542F_manual, ABAC_2809913540_Paint_spray_gun_G-540F_quickguide_and_DoC, ABAC_2809913403_Chisel_hammer_G-475_manual, ABAC_2809913501_Air_gun_G-502_quickguide_and_DoC. Thanks. i accidentally locked my brand new oilless air compressor regulator knob how can i unlock? We also service and install compressed air systems, any problems please contact me personally on 01582 495151 thank you paul alexander. An overheated air compressor is the result of internal factors, external conditions or sometimes both. We have a highly qualified and experienced team of in-house engineers that provide quick, quality solutions at your doorstep. 3. And yes, often that fitting will have a port on the side of it to allow a line to plumb over to the pressure switch unloader valve. Please use the search box or the pages with links to locate and read them. 1. Thanks. We also service and install compressed air systems, any problems please contact me personally on 01582 495151 thank you paul alexander. Yes, youve got a slurry of water / oil and gunk in the tank. Motor turned on no problem. I acquired an ABAC B2800 compressor 2 years ago free of charge because the main bearing had collapsed on the pulley end and the company that owned it felt it would be more efficient to replace than call out an engineer. My compressor starts and runs for about a minute then it sounds like its seizing getting slower and then stops, if i then drain down the air its runs normal again for a minute then does the same again. I have replaced the check valve and unloader valve, Belt is properly tensioned. Im stumped. It sounds like your air demand for the carving tool exceeds the capability of the compressor to provide sufficient air for the period you need it without allowing it to cool. Make, model, air pressure in tank when it stops, does it start OK at the same pressure, when it stops is the tank pressure always the same when it shuts down? I would let the compressor pump the tank up to cut out pressure, crack the tank drain enough to allow a little flow, and let that new air drive the puddle on the bottom of the tank out the drain. Thanks. If I run it with the tanks open the motor continues to run fine. Any ideas? Putting a regulator at the tank, and another at the point of use may lead to an air starvation at the point of use, depending on the regulator settings. Now this copper tube to the upperCooler fitting gets really hot once running more than one cycle will burn you. I run beads on the insides of the aluminum C channels to fill in any high spot off the shroud so it sit tight. If the specific manual you are looking for is not present do not hesitate to contact us. The GENESIS compressor is ideal for OEMs and the medium size industrial and assembly aplications. Please refer to photos. Limit air usage to compressor capacity by using fewer or smaller tools. Share. We also service and install compressed air systems, any problems please contact me personally on 01582 495151 thank you paul alexander. Made jumpers & bypassed pressure switch. "logo": "https://www.abacaircompressors.com/etc.clientlibs/settings/wcm/designs/abac/clientlib-preloaded/resources/img/png/logo.png" Other than that, trial and error. If you are OK with removing the manifold cover, maybe leaving it off, and plumbing in a standard, off the shelf, $15 general purpose regulator that you can acquire from almost every shop that sells compressors as a replacement, your options seem limited. Also the compressor turned freely by hand., prior to having it checked. Now it wont. Sure Steven. Air in tank (as little as 20 PSI), high and low pressure lines connected-> motor will start, strain, and then stop, 3. Parameters before startStrainer Inlet cleanOil level OKOil = BRAND new as FACTORY OIL, Parameters I check during I runningHP-with in the specsLP with in the specsOil level- OK. Not knowing the make or model of air compressor makes the possibility of anyone helping with the problem impossible. The muffler keeps getting filled with gasoline,why would that be? (Post was moved to this location.). Pipe air intake to less humid air source. What am I doing wrong??? Let us know what you found, would you? I have a briggs and Stratton air compressor that I bought last year.the model# is 074079-00. it now only builds pressure to about 70psi. So continuity was checked through each wire & terminal, through the disconnect switch terminals & the pressure switch. Before tackling that, pull the tank check valve and ensure that it is not blocked in any way, will you? The set up 3/8 was not sure that 3/8 head hole going with the up size 3/8 fitting to 1/2 to compression fitting of 1/2 copper would not make the reed valve work harder. Really, its the buildup of the air pressure in the tank that develops as the compressor pump dumps more and more into the tank that you want to be concerned about, and that will not be negatively affected by the size of the tube as far as Im concerned. What are you looking for when it comes to maintain and repair your air compressor? Do the further checks, and please advise what you found. Heres Why & How to Fix, DIY Water Separator For Compressed Air Lines How to GUIDE, Fixing a Leaky Air Compressor Hose How to Guide, Information on Charge Air Pro Air Compressors. The regulator knob has been replaced once but it only worked for a short time. Sorry about your motor. This one Ive no idea, Juan. Lubed air compressors require longer and more frequent operations compared to oil-free ones. See the page Ive moved this post to, and contact Abac directly with your model. How you plumb it, or plug ports into it, is entirely up to what you need to add to the tank. Receiver pressure builds up quickly on compressor. I acquired an ABAC B2800 compressor for free a few years ago and after changing crank bearings has been running well. While increasing the size of the regulator to full size may provide marginal flow improvements, if the compressor is designed to output 5 cfm at 90 psi, thats what it will put out, not more than that. Worn or broken low pressure intake or discharge valves. Remove the compressor cylinder head and inspect for foreign matter on top of the piston. It has no check valve and the main compressed air outlet from the pump goes straight into the tank. It may also be a good idea to replace your. Your post was moved to this page as we couldnt determine what it is you were looking for with regards to your compressor. I checked voltage across the pressure switch and everything reads 125v. Thank you. I saw a modification where someone had this same compressor and changed the regulator to an 80cfm @100psi. And, when air is coming from the tank, it has water in it? Would this tube size tube hurt the pump taking too much compressed air out of the pump too fast. The motor started and stopped with no problem. Let our app guide you through the critical operations needed for your product. Further, the output of the compressor is limited by the fact that the motor is 115 V. Going to a larger regulator will do little to improve the flow. As to the bogging down, Id check the capacitor if it were me. They said nothing was wrong with the motor. 5. I know of no air intake on a normal compressor motor, though they often have grills to allow air to circulate. These link to the most popular products in that category, Choose Options Compare. Will try to have it back online asap. Im sure it needs new oil, etc.2) Do you think the bogging down is being caused by the belt tension? Over an 8-hour period the tank completely depressurizes. Abac compressors offer compressed Air. Print. the flapper valve of my compressor is broken so i change the whole compressor to repair the broken compressor, and by just over night when i check the new installed compressor it turned out that the BRAND NEW installed compressor encountered same problem. My goal is to share knowledge about industrial air compressors and compressed air systems: to make compressed air understandable for everyone! Every detail at your fingertips! Ashely, if nothing else has happened regarding location of use etc., the certainly suggests that the run capacitor on the motor may be failing. The next would be the stock built small REG. I drained the air, did the same test and realized it was bogging at closer to 40 psi. Guide, Using an Air Compressor to Clean Your Computer [GUIDE], Air Coming Out the Intake Filter on Air Compressor? My shutoff Id 120 psi. Attached at end of copper piping run.Question:1) Am i making a mistake by installing a combination water trap/air regulator at the compressor tank? English. I have noticed that when the psi rises to 75 the compressor seems to slow down or start laboring. Could you also add a photo of your Sealey compressor? The lower support is mounted to the back of the handles bolts. Anyone else have some thoughts for Joe on this? 1. Turned it on the other day and left it to build pressure but on my return there was little pressure and the motor had gone out on thermal. The motor should have enough power to pump with back pressure due to the new capacitors. Pump stops for second, motor stops turning more info please? Have an Hitachi hot dog or twin tank small job site compressor. Strong, reliable and operator-friendly, these screw compressors provide effortless operation for years. Bleed tank! You sure seem to be pretty knowledgeable about compressors. Has done well until about a month ago, when I noticed a fuse was blown in the disconnect switch.. I fear Im not understanding the question. I then turned off the motor, drained the tank to 80 PSI. Loose pulley, flywheel, belt, belt guard, cooler, clamps or accessories. 33 gal Craftsman compressor keeps tripping the breaker? i have a very old compressor its a curtis model 40 and it has a setup wherein weights on the pump flywheel move out by centrifugal force and they open or close, I think what is basically an unloader valve at the top of the pump valve head, that is how it is supposed to work. What might the problem with my compressor be? Perhaps you might check the tank drain valve to be sure its shut tight? I do see and hear exactly what you are referring to, Tony. Choose one of the products to go directly to the manual for this product. a. Check for worn crankshaft, keyway or pulley bore, resulting from running with loose pulleys. continuous duty at 175psi.2) Aftercooler manifold 3/4 type L copper piping, 72 total run ( See attached picture)3) Air line from aftercooler manifold 3/4 type L copper, 20 total run.4) 3/4 combination water trap/air regulator, 11oz bowl make, THB installed at compressor tank..5) 3/4 air filter system including water trap/air regulator, coalescing filter and desiccant dryer 11oz bowls. Question Title: ABAC compressor fault; Asked by: Guest; Asked On: 16-08-2015 01:33; Hi I am desperately looking for help. Hi Would the exact motor need to be installed or are there options? Here are a few more air compressor problems and some things to try on your own to fix them: Oil in reservoir has a milky appearance: air intake needs to be less humid to reduce air in the oil. By putting in a inline check valve around the cooler it trap the compressed air at the cooler, making the line all most the same length as the factory one from the head to the tank. And, again, I wouldnt put a regulator there it were me. Even though a lot of manuals are already available the page is updated constantly, check this page for new documents every now and then. Hi, I have a 3HP 20A 135 PSI air compressor. I recently acquired a new to me vintage Kellogg American B321 compressor. I took your suggestion and purchased a water-trap to replace the water-trap regulator combo I originally installed at the air compressor tank. Stay oil-free. I got it non working for a deal but have never gotten it to work. There are also many links to items within our online store. You have a compressor that was built on a Monday or Friday (:-), or how are you getting power to the compressor. Hi David. It seem to develop resistance to spinning while it builds pressure. Learn about industrial compressed air systems and receive fresh articles in your inbox. Hi All Hoping for some help on a little problem. I have a Ingersoll-rand model T30. If all these are OK, then I would be concerned about the motor itself being the issue and you may need to get a load test done on it. 5. In any case, dum question, but with the red ring now touching the black knob, can you rotate the red ring clockwise as far as it will go, and then, can you push down on the black knob to see if that allows the handle to engage with the gearing inside? On closer inspection the oil in that motor was really dirty so I drained it out. ABAC Catalogue 2021: all the compressors, tools and accessories your business needs. And if you have a tip for another compressor user? Then, in time, once that all was voided, most of the oil and crud would be gone and I would shut the tank drain again. They are not the same for every compressor however, and since you dont tell us the make or model, no way can we check. I have tried everything I can think of. From old photos on the internet of similar compressors, it looks like these used to connect into the tank too via a separate connection. Sounds like it could be a capacitor problem. Air in tank, high pressure line connected, low pressure line disconnected-> motor will start, strain, and then stop. Motor will eventually get the compressor to about 110 PSI and then slow down, strain, and stop. Would like to add a filter too. Thinking of returning it, starting over with another one. I have changed the oil and cleaned the air filter. Century AC Motor AO Smith with a R56Y frame. If none, empty the tank, pull the tank check valve and make sure its not compromised allowing air in but not out. I hope another visitor can comment. Thank you very much for your help and suggestions for setting up my air lines and regulators. Amazing. Typically the cooling fan is attached to the same shaft at the drive shaft for the pump. For the 1/2 air hoses run up to the ground floor out the wall to mounted 1/2inch water trap and 1/2inch regulator movable mounting board bracket station I made up. My compressor ABAC has been out of use for 7 years.How do I re-commission it without incurring a massive Repair bill.Also would someone please supply a wiring diagram.Start Run with a capacitor. Turned on the motor and it was straining and unable to turn the compressor. Adding a larger regulator shouldnt be an issue. Please provide more info, Steve. Drain oil, refill with oil of proper viscosity. Thanks for the photos, Dave. Even though a lot of manuals are already available the page is updated constantly, check this page for new documents every now and then. In other words, the back-pressure exceeds the ability of the motor to overcome the problem, and the motor struggles, or, the motor itself is failing and hasnt the ability to develop enough force to overcome load. Air Compressor Troubleshooting Guide. Should I take out the top of the tank check valve or can I just leave it in the system? A higher downstream flow isnt an issue except that it will drain the tank faster and cause more rapid cycling of the compressor motor and pump. }. 3. When open the air locker water will come with air in borewell compressor why. If it isnt the motor itself, the only other thing in the air path from the compression area to the tank is the high-pressure valve or valve plate. Replacement ABAC American Air Compressor Parts Call us for pricing on Air Compressors, Lubricants and Parts! Thank you. Can someone help me out here.I dont understand whats going on? Many thanks. I have a Sealey 3hp 200l compressor which has been stood for 9 years. It could also be binding of the pump piston itself, which, when you remove the belt, removes the load on the motor. Please see the page on this site about air compressor motor capacitors and how to test them. Perhaps you might add that information as a comment, and also please upload at least one photo of your compressor so we can see it. In these troubleshooting 'basics' series I explain the most common problems and their solutions. 2. The flowing of air down the lines will eventually drive debris ahead of it and out the end. Its the compressor thats sold with this tool. Improve ventilation or relocate compressor. This is as far as I have gotten as I cant seem to find anybody in the UK the will service it. I reinstalled the main air filler tube and removed the smaller unloader valve tube. Air in tank, high pressure line connected, low pressure line disconnected-> motor will start, strain, and then stop, 4. I noticed the belt was starting to crack so replaced it and adjusted the tension so that is has about 1/2 of deflection at the midpoint. There are also many links to items within our online store. Specs to comply need to be 1 horsepower, meet rate of 3 scfm @ 40 psi. It was still hooked up on the test bench & they showed me that it would run, but no load was put on it. Hi, I have a twin 4hp motor compressor 47cfmIts not been used that much but the other day one of the motors was red hot and the rubber air intake was melting. Probably just need a new motor. If you do that, adjust the cycle frequency and drain open time to allow each cycle to drain all the water each time it cycles. I know the hole on the left will be fitted to the compressor pump with a check valve. 4. Im kind of lost at what it could be. Of course, the stuff coming out will stain cement and wood floors, so put a catchment under the drain. Hi i spray wd40 on my air crompresser now it doesnt work any advice. If you wish to pose a question to other Abac compressor owners, you can do so using the comment form below. In stock form it only puts out 5.0cfm @90psi and 6.0cfm @40psi. You are referring to an air compressor motor, yes? Anyway that's the. Always remember to check your owners manual to ensure that the correct parts are purchased. We also service and install compressed air systems, any problems please contact me personally on 01582 495151 thank you paul alexander. We have an industrial air compressor that we use in several areas of the shop. Quote:The first thing Im puzzled about is why an after-cooler? Have tried getting pliers, needle nose vice grips, screw driver, even drilled hole through hub cap to solid axle trying to weaken the integrity of it. Add a new gasket and reassemble the head. "@context": "http://schema.org", I have it all on 1/2off the compressor 120psi to cabinet, and at the cabinet reg turned down to 40psi and water trap in to cabinet. 2. Ran well until now? Turned it off. ABAC knows this very well, this is why a wide range of spare parts at your beck and call: new or old replacement parts, piston or screw compressor ones, for oilless or oil lubricated air compressors, we have them all. I then replaced the unloader valve, again, the motor was straining with 80 PSI in the tank. When I pull the string or crank it fills the muffler up with gas. Quick view. Motor turned on no problem. What are possible issues for me to inspect? Terence, is it taking much longer to fill up to the cut out pressure than normal? Did you solve your problem? Its my experience that the pump doesnt care about the size of the outflow tube from the pump head to the tank. I have an old Emglo electric wheelbarrow type compressor. If put a in line 1/2 check valve before the cooler this may cut down the line length for the loader speed up the pressure release to the head. I have a very old compressor (areograph) that Im trying to restore. Well, since its a Clarke, can they not help you find service? Is there an issue with the line that could cause multiple air guns (including a brand new 300$ panther adhesive gun) to leak glue? You are certain that the start cap is the same rating as the original? One of the huge benefits of dealing with a professional company is their support. If that end of the air hose happens to be an air tool or valves or some such, thats where the crud will go. Turned it back off. With luck, a kind Abac owner will have experienced the issue with their compressor that you are having with your Abac, and add some information for you. Clean cooling surfaces of cylinder, intercooler and discharge tube. Wish youd uploaded a photo or two. If not, youll need to look closely to find where the air is escaping from. Knock occurs while compressor is loading. Ive soaped every fitting, tightened those which were leaking. It releases the pressure on the head and the line seam to let more of the air in the head to the tank get in the tank,( as it seem to be a smaller amount let off to waste. Heres where you can find the answer or post your own question about that brand if no answer if desired! I have not gone into the guts of the compressor yet, change the oil, etc. .. Its flapper valve got broken, same as the one i changed. And why, when your Campbell Hausfeld tank pressure drops to the normal cut in point would you not want it to start again? USE ONLY GENUINE REPLACEMENT PARTS If the pump is fine, if the line to the tank is fine, if the tank check valve is fine, if there are no mechanical impediments to stop the pump with low pressure in the tank, then its pretty much got to be a problem with the motor. Turned it off, and when I tried to turn it back on the motor couldnt get the belt moving.So, couple of questions:1) Does anyone have the old service manual for this girl? Rather than having to manually drain all of those valves, why not gang them all to a single valve to be left open unless necessary to close it and one single electronic auto drain that will cycle as needed and drain air and water for a few seconds or so each cycle? This photo shows one set up, but yours could be entirely different depending on what parts are to be installed in the base of the switch or adjacent to it. Stay risk-free. If so, do you drain the tank to get rid of condensed water? GENESIS Rotary screw compressors. Since then blew several fuses. Thanks in advance for any help. Please provide more information along with a photo or two of the compressor so we can try and help. Hi! Most pages have a comment section where you can leave a question about that specific make of compressor. Maxair has been offering an unmatchable quality of service for decades, both repairing and maintaining air compressors from ABAC and other brands alike. If the pressure valve side has an issue, it is possible that it isnt allowing air into the tank once the back pressure reaches a certain threshold, slowing the pump, eventually stalling it, and overloading the motor as well. Turned it back off. I then removed the unloader tube and again the motor was able to turn on. Good luck, I hope someone has the manual to offer. Disassemble check valve assembly, clean or. I suspect air is coming out of your intake port from start up, but once the pump head heats up, thats warming / heating the lube oil, and thats offgassing smoke thats now visible. fortunately I have been able to use the compressor without the long arm from the flywheel connected to the plunger at the top, since moving the plunger rod up or down had no effect at all. Still blew fuses. The problem I see that ever one has when adding a cooler the extra length tub or hose in there cases is the length tub to the check valve. air out head to cooler out of cooler to high pressure 3 hose to water trap to tank. To continue visiting our website, please choose one of the following supported browsers. This is for now. I just have to time cycle the work and rest time for the temp pump and work at hand so it stays on the cooler side of a hard work out As I have had this compressor since 2005 only ever had it hooked up to110V so far but does come 220 too. You are now on the rotary screw compressor page, but there's also the reciprocating (piston) compressor page and the portable (diesel) compressor page. Check for leaks or restriction in hose or piping.

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abac compressor problems